dam ›› 2014, Vol. 0 ›› Issue (3): 8-.
Previous Articles Next Articles
LI Zhi-min, DONG Kai-song, GAO Cheng-zhong, SHEN Wei-cheng and ZHENG Xiang-yu
Received:
Online:
Published:
李志敏,董开松,高承众,沈渭程,郑翔宇
作者简介:
Abstract: The paper introduced the sudden drop of confined water level in the foundation of Liujiaxia Dam and analyzed the change law. Further, it was pointed out that it may caused by crack opening or the connection of crack with seepage passage or the drainage passage. As well, it was advanced that the connection of confined water and fracture water would not be a threat to the dam safety.
Key words: confined water in dam foundation, sudden drop of water level, change law, reason analysis
摘要: 介绍了刘家峡坝基承压水力突降情况,分析了承压水变化规律,揭示了承压水位突降是由于裂隙突然张开或裂隙的某一部位突然与相邻的上部裂隙潜水渗流或排水通道相连通造成的,阐明承压水与裂隙潜水的连通一般对大坝的安全不会构成威胁的观点。
关键词: 坝基承压水, 水位突降, 变化规律, 原因分析
LI Zhi-min, DONG Kai-song, GAO Cheng-zhong, SHEN Wei-cheng and ZHENG Xiang-yu. Analysis on the reasons for sudden drop of confined water level in the foundation of Liujiaxia Dam[J]. dam, 2014, 0(3): 8-.
李志敏1,董开松1,高承众2,沈渭程1,郑翔宇1. 刘家峡水电站坝基承压水水位突降原因分析[J]. 大坝与安全, 2014, 0(3): 8-.
0 / / Recommend
Add to citation manager EndNote|Ris|BibTeX
URL: http://magtech.dam.com.cn/EN/
http://magtech.dam.com.cn/EN/Y2014/V0/I3/8