ISSN 1671-1092 CN 33-1260/TK

大坝与安全 ›› 2023 ›› Issue (6): 57-.

• 资料分析 • 上一篇    下一篇

某混凝土拱坝水平位移异常原因分析

余成钢,曾  超
  

  1. 杭州国家水电站大坝安全和应急工程技术中心有限公司,浙江  杭州,311122
  • 收稿日期:2023-05-11 出版日期:2023-12-20 发布日期:2024-03-07
  • 作者简介:余成钢(1985— ),男,安徽安庆人,高级工程师,主要从事大坝安全管理及安全监测工作。

Analysis of abnormal horizontal displacement of an arched concrete dam

YU Chenggang and ZENG Chao   

  1. Hangzhou National Hydropower Station Dam Safety and Emergency Engineering Technology Center Co., Ltd.
  • Received:2023-05-11 Online:2023-12-20 Published:2024-03-07

摘要: 从地质条件、坝基扬压力、坝体温度场及运行工况等角度,对某混凝土拱坝水平位移异常原因进行综合分析,得出异常水平位移主要为不利工况(包括低温季节水位骤升、气温骤降+水位上升)导致的测值突变,实测径向位移未超过设计计算结果,为日常运行管理提供优化建议。

关键词: 拱坝, 径向位移, 监测数据, 异常分析

Abstract: From the perspective of geological conditions, dam foundation uplift pressure, dam body temperature field and operation conditions, comprehensive analysis of the causes of abnormal horizontal displacement of an arch dam is carried out. It is concluded that the abnormal radial horizontal displacement is mainly caused by the unfavorable working conditions, including the water level surge in low temperature season as well as water level rise during sudden drop of temperature. Furthermore, the measured radial displacement does not exceed the designed calculation results, which may provide optimization recommendations for daily operations.

Key words: arch dam, radial displacement, monitoring data, analysis of abnormal data

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