ISSN 1671-1092 CN 33-1260/TK

大坝与安全 ›› 2023 ›› Issue (1): 50-55.

• 补强加固 • 上一篇    下一篇

白沙河水电站大坝渗漏治理技术

王林林
  

  1. 杭州国电大坝安全工程有限公司,浙江 杭州,310030
  • 收稿日期:2022-07-25 修回日期:2022-08-23 出版日期:2023-02-10 发布日期:2023-04-18
  • 作者简介:王林林(1981—),男,浙江慈溪人,高级工程师,主要从事水利水电、市政交通行业的除险加固工程设计和施工工作。

Treatment measures of dam leakage at Baishahe hydropower station

WANG Linlin
  

  1. Hangzhou Guodian Dam Safety Engineering Co., Ltd.
  • Received:2022-07-25 Revised:2022-08-23 Online:2023-02-10 Published:2023-04-18

摘要:

白沙河水电站自运行以来,大坝渗流量一直高于国内同等规模面板坝,影响工程正常运行。综合检测、检 查及渗漏成因分析后,采取了周边缝集中渗漏点水下灌砂及灌浆、基础水下帷幕灌浆、接缝表层止水更换等治理 措施。从目前运行情况来看,治理效果良好。笔者对治理技术进行了总结,为类似工程渗漏治理提供参考。

关键词:

Abstract:

Since the operation of Baishahe hydropower station, its dam seepage had been greater than that of face slab dams of the same scale in China, which affected the normal operation of this project. After comprehensive detection, inspection and the analysis of leakage causes, treatment measures were adopted such as underwater sand filling and grouting at leakage points of peripheral joints, underwater curtain grouting of dam foundation, and replacement of the watertight seal on joint surface. Concluded from the current operation, the treatment effect is good. The author summarizes the treatment measures, which can provide reference for leakage treatment of similar projects.

Key words: dam leakage, reinforcement grouting, plugging, surface watertight seal, crack treatment

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