ISSN 1671-1092 CN 33-1260/TK

• 资料分析 • 上一篇    下一篇

汶川地震对陈村坝基渗流影响分析

邢林生1,周建波1,汪正春2,孙萍2   

  1. 1.国家电力监管委员会大坝安全监察中心,浙江杭州 310014;2.大唐陈村水力发电厂,安徽泾县 242500
  • 出版日期:2011-06-28 发布日期:2011-06-28

Influence of Wenchuan earthquake on foundation seepage of Chencun dam

XING Lin-sheng, ZHOU Jian-bo, WANG Zheng-chun and et al.   

  • Online:2011-06-28 Published:2011-06-28

摘要: 汶川地震发生后不久,陈村大坝坝基帷幕后部的浅层扬压力测孔和深部排水测孔水位普遍下降,坝基渗漏量显著增加,表明坝基岩体和帷幕受地震影响微细裂隙张开,渗透性增强。坝基经过丙凝化学加强灌浆的部位,测孔水位下降幅度较小,水位恢复过程较快,显示出丙凝化灌的优异防渗和抗震性能。汶川地震对陈村大坝的稳定以及坝基岩体和帷幕没有产生损坏,震后约9个月坝基整体防渗功能已基本恢复。

Abstract: Soon after Wenchuan earthquake, the water levels of shallow uplift pressure and deep drainage observation holes at rear curtain of dam foundation declined, and dam foundation leakage increased significantly, which indicated that, because of earthquake, the micro-cracks in dam foundation rock and the curtain opened wider and permeability was enhanced. At the dam foundation part once acrylamide grouted, the water level stayed higher and recovery process was shorter, which showed that acrylamide grouting was of good seepage-prevention and anti- seismic effect. Wenchuan earthquake did not cause damage to dam stability, foundation rock mass or the curtain. About 9 months after the earthquake, anti-seepage performance of dam foundation recovered.